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Helion Energy Shielding Structure -Foundation February 1, 2023 <br /> Helion Energy <br /> 4. Action Item 4(Resolved)—Side faces of the exposed building column footings were uncovered.Although the <br /> contract plans did not show continuation of the joint filler along the sides of the footings,this was discussed <br /> with Andersen Construction while on site and the exposed faces were covered with plastic sheeting. All <br /> instances appeared to be corrected prior to leaving the site. See Figure 5. <br /> 5. Action Item 5 — Installation of the #8 bar pairs was partially complete during the site visit. The remaining <br /> pairs of bars should be installed prior to placement of the top mat. See Figure 6. The global placement of <br /> the bars was not measured while on site to verify location relative to the future anchor bolt installations. <br /> Andersen should confirm locations of the#8 bars prior to placing the top mat. <br /> 6. Action Item 6 — Instances of (3) bar splices were observed while on site near the SW slab corner. Splices <br /> using(3)bars is acceptable,however,should be re-arranged to not leave gaps between adjacent bars,where <br /> minimum bar spacings are not met. It is also advised to add supplemental tie wire locations at the transition <br /> point of the splice. See Figure 7. <br /> 7. Out-of-Conformance Item 1— Remnants of tie wire and mylar sheets that have fallen to the bottom of the <br /> excavated slab area should be cleared and removed prior to the concrete pour. <br /> 8. Out-of-Conformance Item 2— Instances of mylar sheets that had fallen out of place were observed at a few <br /> locations on the bottom mat. The fallen mylar sheets was discussed with Helion Energy prior to leaving the <br /> site and was confirmed that minor instances of missing sheets was acceptable. <br /> Additional Notes/In-Conformance Items: <br /> 1. General spacing of rebar, on average, was acceptable. <br /> 2. Footing dimensions, width, and depth, were acceptable. <br /> 3. Lap splice lengths were measured in field and were acceptable. <br /> 4. Bottom mat reinforcing at the exposed building column locations except as noted in Action Item 2 were <br /> acceptable. <br /> Hayden Leblonde of Andersen Construction and Paul Gentsch of Helion Energy were on site at the time of the <br /> observation and was notified of the above-mentioned action items.The additional notes were briefly discussed <br /> but have been expanded upon in this report with supplemental information. Once action items and out-of- <br /> conformance items are updated, repaired, and reviewed the structural elements should be in substantial <br /> compliance with the structural contract documents. <br /> Thank you and please call if you have any questions. <br /> Sincerely, <br /> Mackenzie Lostra, PE <br /> Project Engineer <br /> Peterson Structural Engineers Inc. <br /> Sent via email to Paul Gentsch on 2/1/2023 <paul@helionenergy.com> <br /> PAGE 12 <br />