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Geotechnical Engineering Report <br /> Proposed New Storm Water Vault <br /> Northwest Mitsubishi <br /> Novembcr 18, 2002 <br /> CG Pile No. 1397 <br /> Page 4 <br /> 631.5 feeQ. Aclow the fill was a weathered zone that was loose to medium dense wiih trace <br /> organics. The surface water was trickling into the tcst holes and the excavated material was wet <br /> and ran into the excavation. Iivaluation of the bottom of the holes was JitficulL [n Test Pit t at a <br /> depth of 8.5 feet, the material appcared to be a b�ray sand wiPi silt to silty sand that was medium <br /> dense to dense. "Cest Pit 2 could not bc advanced into medium dense or better soils. It was not <br /> possible to detcrminc thc amount of subsurfacc watcr sccpagc in the holcs. <br /> CONCLUSIONS ANll RECOMMENDATIONS <br /> General <br /> The sile is considercd suitaUle for the planned improvements. The nati��e soil at depth appcars to <br /> be mcdium dense to dense soil that should provide good support for the planned strucwre. We <br /> expect that, due to �vct conditions and the depth to medium dense or better soil, some <br /> overexcavation under the vault and replacement with rock matcrial such as 2- to 4-inch rock <br /> spalls will be needcd. 1��c recammend that budgets plan for at least 9-inches of rock undcr the <br /> slab areas and at �cast 18-inches of rock under the footing areas. The rock spalls coutd be cappcd <br /> with 2-inches of tiner crushed rock for a better working surface. 'Che rock luyer may also be <br /> needcd duc to tf�c depth to suitable Uearing soil. Our explorations indicated that the elevation of <br /> suitable mcdium dcnse or better soil may be slightly bclow the planncd Pooting location. <br /> Winter scason grading is planned. Most likely backfill will be completed with soils that are <br /> highly moisture sensitive and dif5cult to compact when wet of optimum moisture. The parking <br /> arca crcated by the planned improvcmcnts is expccted to be gravel covered. We ha��c becn <br /> informed that sctHcment of thc backfill would be acceptable and could bc repaircd with importing <br /> of morc gra�cl. <br /> The lateral pressures acting on the structure will depcnd on Ihe materials used. We present two <br /> scts of figures — one assuming relatively poor compaction using silty sand from the site and <br /> importcd into thc site. Another set of figures assumes compaction meets at leasl 90 percent of <br /> maximum dry density based on ASTM D 1557. W� cxpect that compaction to 90 percent a�ill be <br /> difficult to achic��c wiih the planned construction sciiedule and expected conditions. <br /> Cornerstone Geotechnicaf, Inc. 5�l <br /> /!4 / <br />